David Goff, BM-2, BSU-1
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MORE SWAB
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My name is David
Goff, I was transferred to BSU-1 in Aug. 1965 as a
BMSN, and departed in AUG, 1968 as a BM2. During
that time, I was assigned as Coxswain of the SWAB
for a three month period. I was advised that the
SWAB concept was that of two engineers from San
Clemente Island, and the boat was converted there.
The idea, was of a wolf pack of three to five boats,
which would lay up off the coast, waiting on enemy
craft to pass. Other than the main battery system,
the conversion of the boat was rather crude. Leaving
no doubt the craft was not constructed by
Bertram. The Main Battery was of two gyro controlled
nests of seven 57 MM recoilless rifles, with one 50
Cal. machine gun mounted below each nest, which were
used for spotting, they fired tracers only from a
one thousand round magazine which was mounted
athwart ships under the mounting bar for the rifles.
For retreat a 20 MM cannon, drum fed, was mounted
behind the pilot house. The sighting system I am
vague about, but I do recall that it was rather
sophisticated. The rifles were set up with six in a
circle and one in the middle, quite impressive.
The entire hull was lined with radar absorbent
material including the engine compartment and the
engine hatch covers. The material had the appearance
of egg cartons and it was spongy, a couple of inches
thick and gray in color. The rifles were wrapped
with this material also, and the muzzles and
breaches were covered.
If I remember correctly Mike Bowers was the
engineman, when we went on an operation with a
couple of LCSR's out to San Clemente Island to chase
destroyers. The SWAB got within one hundred fifty
yards of the destroyers before being visually
sighted.
I did not have the opportunity to fire the weapons
package. I was informed that they were test fired.
When the full salvo was fired it blew the engine
hatch covers open.
There was only one of these built and it was on the
31 foot hull. I felt privileged to be the coxswain
of such a scary boat. To me it had a lot of
potential.
PROJECT ZULU
I was also in project ZULU Detachment Bravo, I was
the original Coxswain of the Bravo LCPL Mark 4,
sadly I was only in country on that tour for four
months, personal problems in the states cut my tour
short. I remember disliking the armor plated chairs,
where the armor surrounded my head. We had taken
rounds from forward between the boat officer and
the coxswain, and I thought often about a round
rattling around inside that armor plate. I also
remember during construction of the boats one hell
of a case of flash burn I received while helping the
welders in the cabin of the boat putting in the
ceramic armor plate. I had my eyes wrapped for a
week. While in country, we got up one morning and
went down to check on the boats, and there must have
been a few of hundred thousand black beetles on the
outboard side of our support craft and our boats.
During the night they had come from the other side
of the river.
If I recall correctly we used fire hoses to clear
them off. It was amazing, they were inches deep.
SEABLAZER
I did test an evaluation on the SEABLAZER, she was
the prototype for the stabs. She had twin 300 hp
Ford Interceptors with two four barrel carburetors
on each. The outdrives were complimented with a
hydraulic pitch system witch allowed you to change
the degree of pitch on the outdrives when on the
beach. I remember having half or more of the hull on
the beach and changing the pitch, sending more air
and water forward under the inverted V hull, being
off the beach turned and up on step in a minute. The
boat had lead bars installed representing the weight
of Seal Team, weapons, etc.
REDEYE HEAT SEEKING MISSILE
I was on the crew of PTF-13 during surface to air
testing of the REDEYE missile off the coast of Port
Huenme, Ca. in October 1967. I recall tracking the
test plane with the launcher, having to acquire the
target then move the sight line to another part of
the sight, I think it was called super elevating,
before firing. The test were being run in order to
confirm if the weapon would be useful from a moving
surface. It seemed great to me. The test ended
in tragedy for the accompanying pilot and his
aircraft which was I believe an AD1 Skyraider.
Toward the end of the day, at approximately 1730
hrs. the pilot let us know that he was running low
on fuel and needed to stop operations for the day,
as we were also running low on fuel our skipper
concurred and advised the pilot that we would pick
it up in the morning. We thought he had gone back to
his base, and all of a sudden he is coming
straight up our stern from north to south. He was so
low, that if you could have froze him over the boat,
you could have counted the rivets in the body and
wings of the plane. He flew south about a half mile
or so right on the course the 13 boat was on, at
which time he did a 180 degree roll heading right
back at us. All eyes are on the prop driven
fighter as he heads straight for us. He was so low
that he trimmed off six to eight feet of our port
whip antenna and hit the water about a boat length
behind us, skipped out of the water hit the water
again, at which time his aircraft disintegrated in a
large explosion. The crew was completely stunned.
During initial search all that was found was a
section of wing that was to large for us to recover.
We searched until 2400 if I recall correctly. About
2230 we recovered a double hand full of tissue,
which we wrapped in canvas and turned it over to an
ambulance crew on arrival at the pier.
The pilot was a full commander, combat veteran from
Nam in that type of aircraft. Sad day.
I Googled this and came up with a tidbit that was
written in the Long Beach Press Telegram on Oct, 6
1967. It stated that the pilot and plane
disintegrated and that it was going to be
investigated by non other than Capt. Alan B.
Shepard. The news paper does not have archive that
go back that far, but the Long Beach public library
does have this on micro film.
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LCSR STORY
During the summer of 1968 I was assigned as an LCSR
coxswain, not recalling the boat number or who was
crewing with me. The USS Tucumcari PHG-2 arrived in
July of 68 and was the talk of the town everyone
wanted a ride or just to see her. One summer day it
was arranged for several admirals to pilot the
Tucumcari and get a certificate.
My boat was assigned the task of ferrying the
admirals from a yacht club to the Tucumcari. and
back to the yacht club after there ride. We had
delivered and picked up a couple of them, when the
crew decided they were hungry and thirsty, so we
headed over to the Point Loma Fuel Pier to see if
there was a snack bar, after tying up my bow hook
and engineman went up the pier to find some food and
drink, no sooner than they get a hundred and fifty
yards away the radio starts squawking. The Tucumcari
is coming back into the channel and wants my boat on
station in stream to pick up the admiral. My crew is
way up the pier, so I hit the horn and shout at them
to get back to the boat. They start running back and
I think they are going to be back faster than they
actually are, so I light off both the outboard and
inboard engines thinking we will be out of there
quickly. Wrong, wrong, that inboard engine fired up
the creosote on the piling so fast I could not
believe it. The 750 degree exhaust temp was instant.
Luckily there were fuel pier employees close at
hand. the crew jumped on board and threw off the
lines, and as I pulled away there was a considerable
amount of profanity and fist shaking coming in my
direction as they were breaking out the fire
extinguishers. We arrived on station in time to pick
up the admiral, got him on board and was nicely up
on step when both engines flamed out at the same
time.
The LCSR, the slugs they were, just went dead in the
water and the white smoke started rolling up and
filling the pilot area, the admiral was about to
crap in his pants, we were just inundated with
smoke. I had to reassure the admiral that we were
ok, and that we would be underway as soon as the
turbines RPM came down. There was not a whisper of
the fuel pier fire when I got back to the base, so I
guess the fuel pier crew took the fire in stride.
What a fun day.
MST-1 STORIES 1966
THE DUMP RUN
Soon after arriving at the Nasty Base, the snuffy
BMSN I was, as well as being the new guy, I was
given a dump run with two others. We loaded every
thing on a six-by and headed out, upon arriving at
the dump I was taken by genuine surprise when the
women and children surrounded the truck on the way
in and stayed with it until we finally stopped the
truck. I remember we were shouting at them to back
away so we could unload, to no avail. We ended up
firing our weapons in the air, before they would
back away. We started unloading and they started to
move back to junk that we were throwing off the
truck, we had to fire in the air again before we
could continue, this happened a few times before the
truck could be fully offloaded. Very sad, will never
forget that.
THE CENTIPEDE
One wonderful morning at the Nasty Base, myself and
couple of other seaman were working with a BM1 whose
name I do not recall, although he was a big fellow.
Anyway we were working on land close to one of the
piers, the BM1 did not have his trousers bloused.
Mistake! Suddenly he grabs a hand full of trousers
at his right hip and opens his belt and unbuttoned
his trousers, he turned the trousers inside out at
the hip and flipped a large centipede out onto the
ground.After dispatching the centipede he took a
look at his hip and discovered a nice red bight
area. He was an old farm boy and one of the seaman
was also a farm boy so they went to work. The BM1
broke out a case knife, cut a cross in his hip and
the seaman sucked blood out of it a couple of times.
I don't recall if the BM1 had any further reaction.
AMMO RUN
Blas Mojica GMG3 at the time and myself were given a
list of ammo to pickup for the Nastys. So we got a
six-by and went up to the ammo bunker. We had loaded
all the 20 MM. and 81 MM. So we started loading the
40 MM, there were a lot of cans to load, so we
started throwing the cans on the six-by and allowing
them to slide forward on the steel deck of the
truck, every thing was going great until GMG1
Crabtree showed up. He saw what we were doing and
chewed us up one side and down the other. Then he
asked us if we new when that 40MM ammo was made. Of
course we could care less, we just wanted to get it
loaded and back to the boats. Well Crabtree advised
us that the ammo was made during WW2. Doing a
quick calculation, that made the HEPD and HEAP that
we were loading was around twenty two or three years
old. Wow, that's older than I was. Needless to say
we started handling it a bit more cautiously. Fun
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